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Maximum static rpm too low. Low static rpm in Lycoming or Continental aircraft engine.
With fixed pitch airplanes low static rpm is caused by low engine power,
inaccurate tachometer, or incorrect or mispitched propeller. While constant
speed aircraft engines can suffer the same problems the diagnosis is more
difficult.
If a constant speed propeller airplane won't reach red-line rpm in cruise
then the propeller governor is holding back the propeller and your problem
is not low engine power. At cruise (or descent) even an engine with low
power will turn a propeller past red line because of the low engine loading.
Governor has high rpm stop, propeller has low rpm pitch stop. Either the
propeller or the propeller stop may limit maximum static rpm.
To determine
which is causing trouble, open the throttle and move governor control back
and forth slowly. If maximum static rpm is reached before governor stop
is reached, propeller low pitch stop is probably limiting the rpm. If this
is the case, turn governor high rpm stop out, loosen blade clamp outer
bolts and rotate blades in clamps. Reduce blade angle about 1 degree for
each 100 rpm increase. (1 degree equals 1/32 inch circumference at blade
root.) After blade clamps are tightened, check to see if maximum static
rpm is reached before governor stop is reached. After proper blade angle
is set, reset governor high rpm stop. If maximum static rpm is reached
at same time as governor high stop is reached, governor stop is probably
limiting the maximum rpm. Readjust governor stop to obtain proper rpm.
Turn stop screw out to increase rpm. Inability to attain positive high
pitch can be caused by the high-rpm screw adjusted too far in, causing
restricted arm travel. Remove control arm and rotate one serration clockwise.
Back out high-rpm screw as required (one turn equals 25 rpm).
1. Incorrect system rigging.
2. Low engine power.
3. Erroneous reading tachometer.
4. Sticky pilot valve.
5. Insufficient oil flow to the propeller. With Lycoming aircraft engines you
need to check main bearing clearance and rear plug in center of crankshaft
for blockage. Remove propeller governor. There's a passage that goes down
to the center of the front main bearing. The big hole indexes to the oil
transfer tube which goes to prop governor. Take a differential pressure
tester and with a rubber end push against this passage. Apply 40 pounds
in and as oil blows out of bearing you will see the secondary gauge come
down. After 15 or 20 seconds you want to see 5 to 20 pounds. If you get
very little leakage, say 30 pounds, then this means that oil pressure from
the governor can't get to the propeller to provide control. This is a quick
and easy test to do after engine assembly at overhaul of your Continental or
Lycoming aircraft engine.
6. Loose carburetor bowl attachment bolts allowing air to suck into carburetor.
7. Camshaft lobes ground down.
8. Weak or broken valve springs
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Description of symptom
The major problem though is low engine
power. I don't have experience with this engines performance prior
to the annual. It came out of a 12 year storage and the pilot who
flew it in stated it was low on power then. The mechanics say it isn't
low on power but I pointed out the engine doesn't approach static R.P.M.
stated by Continental with this engine and prop combination. In fact
according to the power absorption curve for this prop it is lucky to be
producing 50 horsepower out of a 75 HP rated engine and prop. It
flys but just barely. When I tried to explain power absorption to
the A&Ps I was met with blank stares. I noticed the plugs and
exhaust are covered with black soot. The mechanics reset the carb
and now it drips fuel. It drips even worse in flight attitude
and I suspect this may be a contributing factor. Do you offer new
or rebuilt carburetors for this A75. Bigger and better would be
nicer if the engine would benefit from it.
I picked up 50 R.P.M. moving the
muffler inner perforated cylinder away from the discharge pipe which was
an apparent restriction. Now if I can find another 150 R.P.M. in static
I will be happy. Any information on carbs and suggestions would be
greatly appreciated.
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Solution
I found someone more qualified to work
on my J4,.... me. The problem was weak valve springs. 62 years of
heating and cooling caused these 54# springs to lose temper and drop
to 37#. The higher R.P.M. caused valve float and worked like a
governor. Pulls like it is advertised to do now. I am a happy
camper.
Thanks for your time.
Comment
Were the valve springs really 62 years
old!
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Around
18,000 feet you'll begin to breathe with more comfort, so pull the rip cord and
see what's cooking. Start finding yourself a nice soft place to land suitable
for a smart pilot like yourself. Parachute Sense US Navy 1944
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